The importance of the unsteady effects between the casing treatment and rotor is still not clear. Experiments are conducted in a transonic compressor with arc skewed slot casing treatment configurations. The experimental results indicate that the unsteady excitation frequency due to the slot number of casing treatment is one of the most important factors influencing compressor performance. Also, compressor performance can be overall enhanced through optimizing this unsteady excitation frequency. For the transonic compressor herein, peak efficiency, stall margin, and maximum flow mass can be improved by 0.17%, 19.86%, and 0.81%, respectively, at near design rotating speed, which can reach up to 1.13%, 57.84%, and 1.57%, respectively, at part design speed.
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April 2011
Research Papers
Experimental Investigation on the Effects of Unsteady Excitation Frequency of Casing Treatment on Transonic Compressor Performance
Wei Tuo,
Wei Tuo
Beijing Aeronautical Engineering Technology Research Center
, Beijing 100076, China
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Yajun Lu,
Yajun Lu
National Key Laboratory on Aero-Engine,
Beijing University of Aeronautics and Astronautics
, Beijing 100191, China
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Wei Yuan,
Wei Yuan
National Key Laboratory on Aero-Engine,
Beijing University of Aeronautics and Astronautics
, Beijing 100191, China
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Sheng Zhou,
Sheng Zhou
National Key Laboratory on Aero-Engine,
Beijing University of Aeronautics and Astronautics
, Beijing 100191, China
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Qiushi Li
Qiushi Li
National Key Laboratory on Aero-Engine,
Beijing University of Aeronautics and Astronautics
, Beijing 100191, China
Search for other works by this author on:
Wei Tuo
Beijing Aeronautical Engineering Technology Research Center
, Beijing 100076, China
Yajun Lu
National Key Laboratory on Aero-Engine,
Beijing University of Aeronautics and Astronautics
, Beijing 100191, China
Wei Yuan
National Key Laboratory on Aero-Engine,
Beijing University of Aeronautics and Astronautics
, Beijing 100191, China
Sheng Zhou
National Key Laboratory on Aero-Engine,
Beijing University of Aeronautics and Astronautics
, Beijing 100191, China
Qiushi Li
National Key Laboratory on Aero-Engine,
Beijing University of Aeronautics and Astronautics
, Beijing 100191, ChinaJ. Turbomach. Apr 2011, 133(2): 021014 (6 pages)
Published Online: October 22, 2010
Article history
Received:
July 22, 2009
Revised:
August 8, 2009
Online:
October 22, 2010
Published:
October 22, 2010
Citation
Tuo, W., Lu, Y., Yuan, W., Zhou, S., and Li, Q. (October 22, 2010). "Experimental Investigation on the Effects of Unsteady Excitation Frequency of Casing Treatment on Transonic Compressor Performance." ASME. J. Turbomach. April 2011; 133(2): 021014. https://doi.org/10.1115/1.4000581
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