In most dry, low-NOx combustor designs of stationary gas turbines, the front panel impingement cooling air is directly injected into the combustor primary zone. This air partially mixes with the swirling flow of premixed reactants from the burner and reduces the effective equivalence ratio in the flame. However, local unmixedness and the lean equivalence ratio are supposed to have a major impact on combustion performance. The overall goal of this investigation is to answer the question of whether the cooling air injection into the primary combustor zone has a beneficial effect on combustion stability and NOx emissions or not. The flame stabilization of a typical swirl burner with and without front panel cooling air injection is studied in detail under atmospheric conditions close to the lean blowout limit (LBO) in a full-scale, single-burner combustion test rig. Based on previous isothermal investigations, a typical injection configuration is implemented for the combustion tests. Isothermal results of experimental studies in a water test rig adopting high-speed planar laser-induced fluorescence (HSPLIF) reveal the spatial and temporal mixing characteristics for the experimental setup studied under atmospheric combustion. This paper focuses on the effects of cooling air injection on both flame dynamics and emissions in the reacting case. To reveal dependencies of cooling air injection on combustion stability and NOx emissions, the amount of injected cooling air is varied. OH*-chemiluminescence measurements are applied to characterize the impact of cooling air injection on the flame front. Emissions are collected for different cooling air concentrations, both global measurements at the chamber exit, and local measurements in the region of the flame front close to the burner exit. The effect of cooling air injection on pulsation level is investigated by evaluating the dynamic pressure in the combustor. The flame stabilization at the burner exit changes with an increasing degree of dilution with cooling air. Depending on the amount of cooling, only a specific share of the additional air participates in the combustion process.
Impact of Cooling Air Injection on the Combustion Stability of a Premixed Swirl Burner Near Lean Blowout
Contributed by the Combustion and Fuels Committee of ASME for publication in the JOURNAL OF ENGINEERING FOR GAS TURBINES AND POWER. Manuscript received June 17, 2013; final manuscript received July 17, 2013; published online September 17, 2013. Editor: David Wisler.
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Marosky, A., Seidel, V., Sattelmayer, T., Magni, F., and Geng, W. (September 17, 2013). "Impact of Cooling Air Injection on the Combustion Stability of a Premixed Swirl Burner Near Lean Blowout." ASME. J. Eng. Gas Turbines Power. November 2013; 135(11): 111501. https://doi.org/10.1115/1.4025043
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