During the 2003 outage at the Ringhals Nuclear Plant in Sweden, a leak was found in the vicinity of a Control Rod Drive Mechanism (CRDM) housing nozzle at Unit 1. Based on the ALARA principle for radioactive contamination, a unique repair process was developed. The repair system includes utilization of custom, remotely controlled GTAW-robots, a CNC cutting and finishing machine, snake-arm robots and NDE equipment. The success of the repair solution was based on performing the machining and welding operations from the inside of the SCRAM pipe through the CRDM housing since accessibility from the outside was extremely limited. Before the actual pipe replacement procedure was performed, comprehensive training programs were conducted. Training was followed by certification of equipment, staff and procedures during qualification tests in a full scale mock-up of the housing nozzle. Due to the ingenuity of the overall repair solution and training programs, the actual pipe replacement procedure was completed in less than half the anticipated time. As a result of the successful pipe replacement, the nuclear power plant was returned to normal operation.
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14th International Conference on Nuclear Engineering
July 17–20, 2006
Miami, Florida, USA
Conference Sponsors:
- Nuclear Engineering Division
ISBN:
0-7918-4242-8
PROCEEDINGS PAPER
Advanced Pipe Replacement Procedure for a Defective CRDM Housing Nozzle Enables Continued Normal Operation of a Nuclear Power Plant
Geoff Gilmore,
Geoff Gilmore
Climax Portable Machine Tools, Inc., Newberg, OR
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Andrew Becker
Andrew Becker
Climax Portable Machine Tools, Inc., Newberg, OR
Search for other works by this author on:
Geoff Gilmore
Climax Portable Machine Tools, Inc., Newberg, OR
Andrew Becker
Climax Portable Machine Tools, Inc., Newberg, OR
Paper No:
ICONE14-89326, pp. 159-168; 10 pages
Published Online:
September 17, 2008
Citation
Gilmore, G, & Becker, A. "Advanced Pipe Replacement Procedure for a Defective CRDM Housing Nozzle Enables Continued Normal Operation of a Nuclear Power Plant." Proceedings of the 14th International Conference on Nuclear Engineering. Volume 1: Plant Operations, Maintenance and Life Cycle; Component Reliability and Materials Issues; Codes, Standards, Licensing and Regulatory Issues; Fuel Cycle and High Level Waste Management. Miami, Florida, USA. July 17–20, 2006. pp. 159-168. ASME. https://doi.org/10.1115/ICONE14-89326
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