High asynchronous self-excited blade response was observed in a transonic first stage rotor during the evaluation of flutter stability in high forward speed conditions. This candidate baseline rotor stage is a highly loaded, snubber-less bladed-disc configuration mounted in an axial low pressure compressor with tip speed in the order of 400 m/s. During the tests, the high asynchronous blade response was measured by strain gages, tip timing system and unsteady blade pressure transducers, which were correlated with analytical predictions. To alleviate this problem, it was attempted to tailor the first rotor blade configuration alone by adhering to all the constraints such as geometric, aerodynamic matching, material selection and utilising the same dovetail root configuration in the existing disc configuration. While tailoring the rotor blade, the critical blade parameters such as axial chord, thickness to chord, stagger, camber, leading and trailing edge radius were iterated from hub to tip. In the tailored rotor blade, the first flexure mode frequency, 1F was improved by 45% whereas the separation between second flexure, 2F and torsion mode, 1T were improved by over 30% with 4.9% weight penalty. Using the one way fluid-structure interaction approach, the blade incidence variation for different inlet pressure conditions and aerodynamic damping were evaluated using energy method for both the configuration. Blade sets of the tailored configuration were manufactured and tested in a dedicated compressor test facility, where characteristics were generated from 70% to 100% corrected speeds. The rig tests confirmed the predicted compressor performance as well as the improvement of natural frequency using blade mounted strain gages for the tailored blade. Upon the verification in the test rig, the tailored rotor configuration was further fitted in the engine and tested up to 103.3% of its design speed. The blade experienced two different inlet total pressure conditions in the test rig and engine tests. The unsteady pressure transducers and blade tip timing sensors did not show any asynchronous response in the corrected speed range for the tailored configuration. Compared to the baseline rotor blade, this tailored rotor blade demonstrated the absence of asynchronous response in the fundamental flexure mode and also well correlated with the aerodynamic damping prediction by energy method. Using this correlation, it is further analytically demonstrated that the blade will have sufficient aerodynamic damping at higher forward speeds and also minimal incidence variation in these conditions.
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ASME 2017 Gas Turbine India Conference
December 7–8, 2017
Bangalore, India
Conference Sponsors:
- International Gas Turbine Institute
ISBN:
978-0-7918-5851-6
PROCEEDINGS PAPER
Flutter Alleviation by Aeroelastic Tailoring of a Transonic Rotor Blade
Sankarkumar Jeyaraman,
Sankarkumar Jeyaraman
Gas Turbine Research Establishment, Bangalore, India
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Kirubakaran Purushothaman,
Kirubakaran Purushothaman
Gas Turbine Research Establishment, Bangalore, India
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Ramaraja Bhat,
Ramaraja Bhat
Gas Turbine Research Establishment, Bangalore, India
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Kishore Prasad Deshkulkarni
Kishore Prasad Deshkulkarni
Gas Turbine Research Establishment, Bangalore, India
Search for other works by this author on:
Sankarkumar Jeyaraman
Gas Turbine Research Establishment, Bangalore, India
Kirubakaran Purushothaman
Gas Turbine Research Establishment, Bangalore, India
Ramaraja Bhat
Gas Turbine Research Establishment, Bangalore, India
Kishore Prasad Deshkulkarni
Gas Turbine Research Establishment, Bangalore, India
Paper No:
GTINDIA2017-4662, V002T05A012; 11 pages
Published Online:
February 2, 2018
Citation
Jeyaraman, S, Purushothaman, K, Bhat, R, & Prasad Deshkulkarni, K. "Flutter Alleviation by Aeroelastic Tailoring of a Transonic Rotor Blade." Proceedings of the ASME 2017 Gas Turbine India Conference. Volume 2: Structures and Dynamics; Renewable Energy (Solar, Wind); Inlets and Exhausts; Emerging Technologies (Hybrid Electric Propulsion, UAV,..); GT Operation and Maintenance; Materials and Manufacturing (Including Coatings, Composites, CMCs, Additive Manufacturing); Analytics and Digital Solutions for Gas Turbines/Rotating Machinery. Bangalore, India. December 7–8, 2017. V002T05A012. ASME. https://doi.org/10.1115/GTINDIA2017-4662
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