The tip leakage flow which is characterized by the blade tip vortex is a highly complex and unsteady phenomenon. It is of great interest to understand the unsteady pressure characteristics of tip leakage flow. The present study aims to focus on the unsteady pressure behavior caused by tip leakage flow of a single stage axial flow turbine. A series of experiments were carried out with a scaled up high work axial flow turbine in a Large Scale Rotating Rig to understand this unsteady pressure behavior. The pressure fluctuations were mapped at five axial locations on the casing across the rotor tip. Unsteady pressures were measured using calibrated fast response transducers. Measurements were phase-locked with the rotor. The pressure data was ensemble averaged and represented gross unsteadiness in the flow. Experiments were carried out over a range of flow coefficients (Cx/U) like 0.30, 0.32, 0.34 and 0.36. The blade pass frequency was the predominant one seen during the measurements. Mild influence of vane exit wake turbulence was also seen during the measurements. Constant speed flow coefficient variation did not seem to cause additional unsteadiness to the tip leakage flow.
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ASME 2017 Gas Turbine India Conference
December 7–8, 2017
Bangalore, India
Conference Sponsors:
- International Gas Turbine Institute
ISBN:
978-0-7918-5850-9
PROCEEDINGS PAPER
Experimental Study of Unsteady Pressure Fluctuations due to Tip Leakage Flows in an Axial Flow Turbine Available to Purchase
R. Senthil Kumaran,
R. Senthil Kumaran
CSIR-National Aerospace Laboratories, Bangalore, India
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Kishor Kumar,
Kishor Kumar
CSIR-National Aerospace Laboratories, Bangalore, India
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N. Poornima
N. Poornima
CSIR-National Aerospace Laboratories, Bangalore, India
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R. Senthil Kumaran
CSIR-National Aerospace Laboratories, Bangalore, India
Kishor Kumar
CSIR-National Aerospace Laboratories, Bangalore, India
N. Poornima
CSIR-National Aerospace Laboratories, Bangalore, India
Paper No:
GTINDIA2017-4868, V001T02A012; 8 pages
Published Online:
February 2, 2018
Citation
Senthil Kumaran, R, Kumar, K, & Poornima, N. "Experimental Study of Unsteady Pressure Fluctuations due to Tip Leakage Flows in an Axial Flow Turbine." Proceedings of the ASME 2017 Gas Turbine India Conference. Volume 1: Compressors, Fans and Pumps; Turbines; Heat Transfer; Combustion, Fuels and Emissions. Bangalore, India. December 7–8, 2017. V001T02A012. ASME. https://doi.org/10.1115/GTINDIA2017-4868
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