An experiment has been conducted to study stator/rotor disc cavity leakage flow on the platform of a highly loaded stationary linear blade cascade. The linear cascade consists of a scaled-up model of the high-pressure turbine blades of an E3 (Energy efficient engine) and leakage slot models installed under the platform. Experiments have been conducted to investigate the effect of the slot injection angle, leakage flow rates, distance between the leading edge of the blade and the slot, and spacing of the blades. The film-cooling effectiveness was measured by pressure sensitive paint (PSP), and the temperature fields and flow fields were investigated using laser-induced fluorescence (LIF) and particle image velocimetry (PIV), respectively. It was observed from the experiments that the leakage flow covered the surface of the blade platform when the distance between the leading edge and the slot was zero; however, with increasing distance, the horseshoe vortex dominates near the junction of the blade leading edge, and the leakage flow could not cover the region. It was also found that the leakage flow has an effect that promotes the formation of the horseshoe vortex for some experimental conditions.
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ASME Turbo Expo 2015: Turbine Technical Conference and Exposition
June 15–19, 2015
Montreal, Quebec, Canada
Conference Sponsors:
- International Gas Turbine Institute
ISBN:
978-0-7918-5672-7
PROCEEDINGS PAPER
Experimental Study of Leakage Flow on Flow Field and Film Cooling of High Pressure Turbine Blade Platform Available to Purchase
Kenichiro Takeishi,
Kenichiro Takeishi
Tokushima Bunri University, Sanuki, Kagawa, Japan
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Yutaka Oda,
Yutaka Oda
Kansai University, Suita, Osaka, Japan
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Shintaro Kozono
Shintaro Kozono
Fuji Heavy Industries Ltd., Mitaka, Tokyo, Japan
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Kenichiro Takeishi
Tokushima Bunri University, Sanuki, Kagawa, Japan
Yutaka Oda
Kansai University, Suita, Osaka, Japan
Shintaro Kozono
Fuji Heavy Industries Ltd., Mitaka, Tokyo, Japan
Paper No:
GT2015-42898, V05BT12A026; 13 pages
Published Online:
August 12, 2015
Citation
Takeishi, K, Oda, Y, & Kozono, S. "Experimental Study of Leakage Flow on Flow Field and Film Cooling of High Pressure Turbine Blade Platform." Proceedings of the ASME Turbo Expo 2015: Turbine Technical Conference and Exposition. Volume 5B: Heat Transfer. Montreal, Quebec, Canada. June 15–19, 2015. V05BT12A026. ASME. https://doi.org/10.1115/GT2015-42898
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