The performance implications of operating on Synthetic-Paraffinic Kerosene (SPK) were investigated using a RR-Allison T63-A-700 Model 250-C18 B gas turbine and compared to conventional Jet A-1. The SPK was aromatic–free and possessed a greater hydrogen/carbon ratio than petroleum derived Jet A-1. The variation in aromatic content had several implications with respect to soot and NOx emissions. Reduced aromatics also implied a reduction in the radiative heat transfer to the combustor liner. A simple model was used to explore the effect of H/C ratio on the adiabatic flame temperature, the combustor exit temperature and the engine efficiency via the impact on the gas properties and these were compared to the experimental data. It was found that operation with SPK changed directionally toward improving energy extraction via a turbine and an overall efficiency gain of about 1.2% was attained with operation on SPK through increased combustion efficiency, a reduction in liner pressure loss and an improvement in the combustion products properties. A modified combustion liner was fitted to enable the thermal loading on the combustor liner to be investigated and the expected trend with the SPK fuel was confirmed and quantified.
Skip Nav Destination
ASME Turbo Expo 2009: Power for Land, Sea, and Air
June 8–12, 2009
Orlando, Florida, USA
Conference Sponsors:
- International Gas Turbine Institute
ISBN:
978-0-7918-4883-8
PROCEEDINGS PAPER
Assessment of the Operational Performance of Fischer-Tropsch Synthetic-Paraffinic Kerosene in a T63 Gas Turbine Compared to Conventional Jet A-1 Fuel Available to Purchase
Nigel Bester,
Nigel Bester
University of Cape Town, Rondebosch, South Africa
Search for other works by this author on:
Andy Yates
Andy Yates
University of Cape Town, Rondebosch, South Africa
Search for other works by this author on:
Nigel Bester
University of Cape Town, Rondebosch, South Africa
Andy Yates
University of Cape Town, Rondebosch, South Africa
Paper No:
GT2009-60333, pp. 1063-1077; 15 pages
Published Online:
February 16, 2010
Citation
Bester, N, & Yates, A. "Assessment of the Operational Performance of Fischer-Tropsch Synthetic-Paraffinic Kerosene in a T63 Gas Turbine Compared to Conventional Jet A-1 Fuel." Proceedings of the ASME Turbo Expo 2009: Power for Land, Sea, and Air. Volume 2: Combustion, Fuels and Emissions. Orlando, Florida, USA. June 8–12, 2009. pp. 1063-1077. ASME. https://doi.org/10.1115/GT2009-60333
Download citation file:
107
Views
Related Proceedings Papers
Related Articles
Comparison of Filter Smoke Number and Elemental Carbon Mass From Partially Premixed Low Temperature Combustion in a Direct-Injection Diesel Engine
J. Eng. Gas Turbines Power (October,2011)
Advanced Catalytic Pilot for Low NO x Industrial Gas Turbines
J. Eng. Gas Turbines Power (October,2003)
Development of a Hydrogen Microgas Turbine Combustor: NO x Emissions and Secondary Air Injection
J. Eng. Gas Turbines Power (February,2025)
Related Chapters
Combined Cycle Power Plant
Energy and Power Generation Handbook: Established and Emerging Technologies
Outlook
Closed-Cycle Gas Turbines: Operating Experience and Future Potential
Introduction
Consensus on Operating Practices for Control of Water and Steam Chemistry in Combined Cycle and Cogeneration